KN
realizes EFM performance value through specialized training
Instructors
covered specifically what technicians need to know for configuring
electronic measurement units
By Arlin Mead and Joe
Sargent, KN Energy, Inc., Lakewood, Colorado
While electronic flow
measurement (EFM) is recognized as a breakthrough technology for natural gas
production, transportation, and distribution companies, placing too much
confidence in the instruments can lead to disastrous results without proper
training in place.
Ironically, field automation,
which is intended to lessen reliance upon individuals, cannot succeed
without enlightened workers in the field who can make the electronic devices
perform as anticipated.
Soon after KN Energy made a
major commitment to EFM, it was determined that simply installing electronic
devices was not enough to achieve the kind of results required by the
company. To obtain the most accurate data on gas flows throughout an
extensive pipeline system, an effective training program was essential to
make it happen.
It was apparent that the
field technicians who were initially entrusted with the new equipment just
didn't fully understand their new jobs. Even though they were able to
install the units in remote locations and get them running to measure gas
flow and transmit data, the units needed to be configured according to
company standards to deliver the level of accuracy the company was
demanding. It was obvious field technicians, who were working with the new
instruments, did not fully understand the need to enter information
precisely according to KN requirements.
Because of this, a major
challenge was developing because KN's plans called for installing hundreds
of remote EFM units from the Canadian border all the way south into Mexico,
using more than 200 field technicians, most of whom had little
instrumentation knowledge. A laptop computer is used to configure these
units, but many technicians had never even turned on a computer previously.
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Training.
Fisher-Rosemount instructor Tim Allen (center) checks work of
two KN Energy technicians learning to use laptops to configure ROC
units. |
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Training
Needed
The company concluded that
this field force could not be expected to service complex electronic
measurement devices without sufficient training. The desired results just
could not be achieved until those men and women fully understood what they
needed to do each time a unit was installed.
As a result, an arrangement
was made with Fisher-Rosemount Educational Services (FRES) for 16 weeks of
training to be conducted at various sites across the operating area. The
training was to be based on the Fisher Remote Operations Controller (ROC),
which had been selected as standard equipment for EFM throughout KN Energy.
The ROC is a complex,
microprocessor-based instrument capable of measuring gas flows and
calculating volumes according to American Gas Association (AGA) formulas.
Depending on the model, these units can measure multiple flows, store data,
and transmit it to a host on a predetermined schedule or on demand.
KN elected to train primarily
on the gas measurement capability of the ROC, instructing field technicians
how to configure each device to ensure transmission of complete, error-free
data in the company format.
The training goal was to:
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Assure the accuracy of
all gas flow measurements
-
Minimize EFM cost by
making field technicians proficient in configuration
-
Reduce cost of checking
for and correcting errors
-
Provide better service
and better data for customers.
Modified
Curriculum
After the initial class, it
was apparent these goals were not being met, because the course was not
sufficiently oriented to the KN Energy requirements. Field technicians had
to learn exactly how to configure the remote units to deliver-error free
data in a unique format. To accomplish this, the training had to be
KN-specific, stressing just what the trainees needed to know without getting
into all the capabilities of the instrumentation. Further, it was important
for instructors to emphasize the importance of proper configuration and the
economic impact of measurement errors resulting from erroneous entries.
KN Energy has a well-defined
way of managing gas flow measurement that gives optimum results. The
training manual and the instruction had to reflect this philosophy. Every
parameter influencing measurement was given a hard look and changes were
made to the basic manual, where necessary, to incorporate company standards.
These changes are highlighted in the manual in bold type following a "KN
Issues" heading. This is a flag to technicians that the following
information is essential for them to know, and there are many such headings
in the new manual.
For example, one section
discusses the importance of entering the correct latitude during
configuration and gives the south-to-north latitudes of the various states
in which KN operates so a technician can select the correct latitude for the
site where a unit is being installed. Another highlighted section discusses
the importance of entering the elevation so that atmospheric pressure is
correct.
Examples showing the cost of
entering a wrong value during configuration were included. For example,
entering a specific gravity value of 0.63 rather than 0.78 can result in a
measurement difference of 291.26 Mcf per day or 8,737.8 Mcf per month, a
dollar variation of $17,475 per month at that one unit. Driving home the
economic impact of tiny configuration errors was a prime objective of this
program.
In class, instructors covered
specifically what the technicians needed to know to properly configure the
ROC units, emphasizing the "KN Issues" sections in the
manual. In the hands-on workshop sessions, each individual had an
opportunity to configure a unit at least four times.
One of the best things the
company did was develop a means of measuring the results of the training to
be certain that the students understood what had to be done each time an EFM
device was installed at a remote site. Every student had to pass a test,
which consisted of configuring a unit using a set of parameters provided by
the instructor. Those who did not succeed with this pass/fail test had to
repeat the training.
Results
About 230 field technicians,
supervisors, and engineers were trained to configure the ROC during the
summer of 1997 with an excellent first-time pass rate of 95%. Most classes
ranged from 10 to 16 persons, and, excluding the initial class, there was
never more than one failure per class. All of those who attended that first
class subsequently passed the test. In fact, with just one exception, every
person who failed once and repeated the training passed on the second
opportunity.
The results proved that
people without computer skills can learn to configure a complex flow
measurement instrument using a laptop computer after just one week of
specialized training. They're not computer literate, but they do know how to
hook up a laptop and communicate with a remote unit to make it operate
correctly. This has resulted and will continue to result in accuracy
improvements that will pay for the training. Within the first thirty days
after training there were enough positive results to call the training
effort a success.
The gas balance of inputs to
outputs throughout KN's system also is improving. However, greater
improvements are possible, and efforts will continue toward achieving better
electronic flow measurement.
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